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dc.contributor.authorCaukill, Mark
dc.date.accessioned2017-04-06T01:55:21Z
dc.date.available2017-04-06T01:55:21Z
dc.date.issued2001
dc.identifier.urihttp://hdl.handle.net/10179/10708
dc.descriptionAppendix F, G and H have been removed due to copyrighten_US
dc.description.abstractPrecision Manufacturing Limited (PML) is a small general engineering firm in Feilding, New Zealand. It is a general job shop (with a few specialty products) well known in the region for producing timely, high quality results. Southchain Conveying Systems Limited was purchased in November of 1998 and is the only conveyor chain manufacturer in New Zealand. Soon after taking over Southchain, the company found it difficult to compete against chain imports in the New Zealand conveyor chain market with a manual operation. At this point in time Precision Manufacturing owner, Garth Thelin, contacted Massey University and the idea of a GRIP project was introduced. The project commenced on November 1 1999 and ran for 14 months. The technical goals of the project were to reduce manufacturing costs by 30% and limit capital expenditure to $100,000. A numerical process model was built using Microsoft Excel based around a combination of a Bill of Materials model and a Route Sheet model. After completing the proccss model, it was then analysed to obtain a list of first order savings projects in the company. Dollar savings vs. the estimated cost of implementation, as well as interdependencies between the issues, was used as a criteria to rank projects as first order. Two projects were then chosen to be pursued: pin induction automation and roller induction heat treatment. The induction automation project covered the design of the mechanical apparatus, building and testing of working models, building of the production machinery, and the industrial control systems to integrate the mechanics to the induction heater. The roller induction heat treatment project investigated using the in-house induction heater to case harden the chain rollers and divest the company of a high external expense. Six months after the project was completed the company had reduced its costs considerably and as a result, was more profitable. The key to this was the reduction in roller costs. With better margins the company has been able to increase its sales and hence boost production levels. Being more profitable also means the company is in a better position to implement more cost saving measures and become more competitive in the market place.en_US
dc.language.isoenen_US
dc.publisherMassey Universityen_US
dc.rightsThe Authoren_US
dc.subjectManufacturing processesen_US
dc.subjectCost Controlen_US
dc.titleIntroducing cost-effective technology into a small New Zealand manufacturing company : a thesis presented in partial fulfilment of the requirements for the degree of Master of Technology in Manufacturing and Industrial Technology at Massey Universityen_US
dc.typeThesisen_US
thesis.degree.disciplineManufacturing and Industrial Technologyen_US
thesis.degree.grantorMassey Universityen_US
thesis.degree.levelMastersen_US
thesis.degree.nameMaster of Technology (M. Tech.)en_US


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